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Deepwater Horizon Deepwater_Horizon - Coggle Diagram
Deepwater Horizon
What Happened
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On April 20, 2010 the incident involved a failure and loss of hydrostatic control of the well
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Summary
Surge of natural gas blasted through a concrete core that was recently installed to seal an oil well which is designed to be used for later oil productions/ retrieval purposes. The Blast occurred due to failures in maintenance, management, testing, and operation
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Why It Happened
- Annulus cement barrier did not isolate the hydrocarbons
The day before the disaster, the cement was pumped down the production casing and up into the wellbore annulus to prevent hydrocarbons from entering the wellbore from the reservoir
The annulus cement placed across the main hydrocarbon zone was a light, nitrified foam cement slurry product
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Weaknesses in the cement design, testing, and quality assurance/ risk assessment was determined
- The shoe track barriers did not isolate the hydrocarbons
Hydrocarbons entered the wellbore annulus and passed down where they entered the production casing through the shoe track
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Hydrocarbon ingress was through the shoe track rather than through a failure in the production casing or the wellbore annulus and going up through the casing hanger seal assembly
- The negative pressure test was accepted although the well integrity test was not established
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The test involved replacing heavy drilling mud with lighter seawater to place the well in a controlled under-balanced condition
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- Influx was not recognised until hydrocarbons were in the riser
As the negative pressure test was accepted, the well was returned to an overbalanced condition, preventing influx into the wellbore
Normal operating conditions involved the temporary abandonment of the well whilst heavy drilling mud was replaced with seawater which under-balanced the well
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Indication of influx as well as increase of drill pipe pressure was not noticed through 'real-time' data which resulted in the crew taking roughly 40mins to act on control measures of the rig
The first control measure by the crew occurred after hydrocarbons were rapidly flowing to the surface
- Well control response actions failed to regain control of the well
The first well control measures were to close the BOP and diverter which routed the fluids to exit the riser to the mud gas separator (MGS) system rather than the overboard diverter line
- Diversion to the mud gas separator resulted in gas venting onto the rig
Once diverted to the MGS, hydrocarbons were vented directly onto the rig through a goose-necked vent which exits the MGS where other flow lines are also directed onto the rig.
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- The fire and gas system did not prevent hydrocarbon ignition
Hydrocarbons migrated beyond areas on the rig that were electrically classified to areas where potential for ignition was increased
Heating, ventilation, and air-con system likely transferred a gas mixture into engine rooms which caused one of the engines to over-speed and result in the source of ignition
- The BOP emergency mode did not seal the well
- Explosion and fire likely disabled the emergency disconnect sequence and primary emergency method available to rig staff which is designed to seal wellbore and disconnect marine riser from the well
- Condition of critical components in the control pods likely prevented activation of another emergency method of well control (Automatic Mode Function- AMF) which is designed to seal well without human intervention during loss of hydraulic pressure
- Remotely operated vehicle intervention to initiate the auto-shear function likely resulted in closing the BOP's blind shear ram 33 hours after the explosions and fire but instead failed to seal the well
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Related Issues/ Elements
People
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Supervisors, Foreman, Leading Hands, Superintendents
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Workplace Environment
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Rig Design
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Job Design
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As part of normal operations to temporarily abandon the well, the crew began to displace the remaining drilling fluid of seawater. The annular preventer was opened and the well returned to an overbalance position preventing further influx into the wellbore
Displacement continued as planned and the well went under-balanced resulting in pressure of the well dropping below the reservoir pressure
Well started to flow and crew emptied trip-tank which likely masked any flow indications on the flow meter
Failure
Constant pump rate pressure should have declined as the mud (heavier) was replaced with seawater (lighter). Instead pressure on drill pipe increased by 100 psi, indicating well problem
Sheen test on spacer is to check that no free fluid will be discharged to the sea. The pumps were shut down when the spacer reached the surface. A machine test was performed and the spacer was determined to be suitable for discharge.
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Mud shot up through the derrick and the diverter was closed so flow was diverted to the mud gas separator when the rig crew closed an annular preventor
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Combustible gas cloud reached the aft starboard quadrant of main deck and entered air intakes for engine rooms. The main power generation engines went into over-speed, shutting off all electrical power and controls.
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Emergency disconnect system did not function when activated and the lower marine riser package failed to unlatch from the BOP which did not seal the well
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Management
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Manage projects, tests, operations etc.
Safety performance, procedures, operations etc.
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Critical decision making
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Emergency disconnect sequence for the BOP was activated from the bridge. While lights changed on the control panel, no flow was observed on the flow meters
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Information Transfer
After second integrity test was conducted, site well leader informed rig crew that negative test procedure needed to be conducted on the kill line
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Drill pipe valve was to be closed, tested, and reconfigured for flow and monitored on the kill line
Kill line valve was opened then closed by rig crew and monitored for 30 minutes for flow but no flow showed
Discussion around drill pipe pressure occurred and the source of the 1400 psi took place where it was explained as a phenomenon called the 'bladder effect;
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When disconnection from the well failed, order to abandon the rig was called
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Sequence of Events
Events leading up to accident (prior to April 19, 2020)
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