Deepwater Horizon Deepwater_Horizon

What Happened

Design Failures & System Life Cycle

Why It Happened

Nature of the System & System Parts

System Parts and Failures

Related Issues/ Elements

Operational Factors

Life Cycle

People

Workplace Environment Design

Management

Hydrocarbons escaped from the Mancondo well onto Transocean's Deepwater Horizon

Resulted in explosions and fire on the rig

Mechanical and Design failures contributed to the disaster

Eleven people lost their lives

17 people were injured

The fire fuelled hydrocarbons from the well which continued for 36 hours until the rig sank

Hydrocarbons continued to flow from the reservoir through the wellbore and the blowout preventor (BOP) for 87 days

A spill was created which was considered a national/ significant event

BP Exploration & Production were the lease operators of the Mississippi Canyon Block 252

BP formed an investigation team and charged with collecting the facts and sequence of events surrounding the disaster

On April 20, 2010 the incident involved a failure and loss of hydrostatic control of the well

Failure to control the flow from the well with the BOP equipment

allowed for the release and ignition of hydrocarbons

BOP functions failed to seal the well after the initial explosion

Fault Tree Analysis applied and found eight key causes of the accident

  1. Annulus cement barrier did not isolate the hydrocarbons
  1. The shoe track barriers did not isolate the hydrocarbons
  1. The negative pressure test was accepted although well integrity test had not been established
  1. Influx was not recognised until hydrocarbons were in the riser
  1. Well control response actions failed to regain control of the well
  1. Diversion to the mud gas separator resulted in gas venting onto the rig
  1. The fire and gas system did not prevent hydrocarbon ignition
  1. The BOP emergency mode did not seal the well
  1. Annulus cement barrier did not isolate the hydrocarbons
  1. The shoe track barriers did not isolate the hydrocarbons
  1. The negative pressure test was accepted although the well integrity test was not established
  1. Influx was not recognised until hydrocarbons were in the riser
  1. Well control response actions failed to regain control of the well
  1. Diversion to the mud gas separator resulted in gas venting onto the rig
  1. The fire and gas system did not prevent hydrocarbon ignition
  1. The BOP emergency mode did not seal the well

The day before the disaster, the cement was pumped down the production casing and up into the wellbore annulus to prevent hydrocarbons from entering the wellbore from the reservoir

The annulus cement placed across the main hydrocarbon zone was a light, nitrified foam cement slurry product

This product likely experience and contributed to nitrogen breakout and migration

This would allow hydrocarbons to enter the wellbore annulus

Weaknesses in the cement design, testing, and quality assurance/ risk assessment was determined

Hydrocarbons entered the wellbore annulus and passed down where they entered the production casing through the shoe track

The shoe rack is installed at the bottom of the production casing

This allowed flow to enter the production casing rather than the casing annulus

This occurs when both barriers in the shoe track fail to prevent hydrocarbon entry in the production casing

The first barrier (cement in shoe track)
The second barrier (float collar)- device that is located at the top of the shoe track, designed to prevent fluid ingress into the casing

Hydrocarbon ingress was through the shoe track rather than through a failure in the production casing or the wellbore annulus and going up through the casing hanger seal assembly

Negative pressure test was conducted to verify the integrity of mechanical barriers

The shoe track, production casing, and casing hanger seal assembly

The test involved replacing heavy drilling mud with lighter seawater to place the well in a controlled under-balanced condition

Pressure readings and volume bled at the same time of the negative pressure test

Indicated flow-path communication with the reservoir which signified the integrity of the barriers was not achieved

The crew and BP site leaders were of the incorrect view that the test was successful and well integrity was achieved

As the negative pressure test was accepted, the well was returned to an overbalanced condition, preventing influx into the wellbore

Normal operating conditions involved the temporary abandonment of the well whilst heavy drilling mud was replaced with seawater which under-balanced the well

This allowed hydrocarbons to flow up through the production casing and pass the BOP

Indication of influx as well as increase of drill pipe pressure was not noticed through 'real-time' data which resulted in the crew taking roughly 40mins to act on control measures of the rig

The first control measure by the crew occurred after hydrocarbons were rapidly flowing to the surface

The first well control measures were to close the BOP and diverter which routed the fluids to exit the riser to the mud gas separator (MGS) system rather than the overboard diverter line

Once diverted to the MGS, hydrocarbons were vented directly onto the rig through a goose-necked vent which exits the MGS where other flow lines are also directed onto the rig.

This increased the potential for gas to reach an ignition source

Hydrocarbons migrated beyond areas on the rig that were electrically classified to areas where potential for ignition was increased

Heating, ventilation, and air-con system likely transferred a gas mixture into engine rooms which caused one of the engines to over-speed and result in the source of ignition

  1. Explosion and fire likely disabled the emergency disconnect sequence and primary emergency method available to rig staff which is designed to seal wellbore and disconnect marine riser from the well
  1. Condition of critical components in the control pods likely prevented activation of another emergency method of well control (Automatic Mode Function- AMF) which is designed to seal well without human intervention during loss of hydraulic pressure
  1. Remotely operated vehicle intervention to initiate the auto-shear function likely resulted in closing the BOP's blind shear ram 33 hours after the explosions and fire but instead failed to seal the well

Planning

Construction

Commissioning

Maintenance

Concept (Detailed Design)

Operation

Infrastructure-led development

Engineering team and subsurface specialists estimate pore pressures and strengths of geologic formations

Shallow hazard assessment and peer reviewed designed completed

Multiple plan stages comprising technical and mechanical review and changes

Final design involved nine casing strings for drilling where plan included eight

Differing pore pressures and fracture gradients resulted from design basis

Mud weights and well casing setting depths changed from original design

Revised casing design was prepared to address high formation pressure that led to well control

Logging and evaluation was achieved to determine reservoir intervals which was followed by a clean-out trip to condition the wellbore and verify operating condition

April 16, 2010, MMS approved procedure for temporary abandonment of well

Sequence of Events

Events leading up to accident (prior to April 19, 2020)

Final Casing Run

Cement Job

Positive Pressure and Negative Presure Tests

Well Monitoring and Simultaneous Operations

Well Control Response

Explosion and Fire

BOP Emergency Operations

Investigation & Conclusions

Drill a well to tap into the reservoir on the Macondo Prospect

Oil is meant to be reached and once this is achieved, the plan is to cap the well column with three cement plugs so that another rig could return at a later time and remove the oil

Operations and design involved sealing the well at approx. 1500m deep in water before oil production commenced

Rig commissioned by R&B Falcon and registered in Majuro before being leased to BP in 2001

Testing

Stablising

Approval

Operating rights

Commenced in December 1998

The Keel was laid on 21 March 2000

Rig was delivered on 23 February 2001

Built by R&B Falcon which became part of Transocean by Hyundai Heavy Ind. in South Korea

Ultra deep-water dynamically positioned

Semi-submersible offshore drilling rig

Wight: 52,590 tons

Length: 112m

Risk Assessment

Well monitoring measures and control practices

Integrity testing practices

BOP system maintenance

Mechanical repairs

Regular equipment inspection

Pre-job inspection, testing and maintenance of blowout prventor

Ineffective Maintenance Management

Batteries in pod fully depleted

No indications that the AMF and ROV intervention systems were tested as required by policy

non-original equipment manufacturer (non-OEM) was found on solenoid valve during examination

History

Testing and modifications conducted since commissioning provides information regarding likely condition of BOP at time of incident

Summary
Surge of natural gas blasted through a concrete core that was recently installed to seal an oil well which is designed to be used for later oil productions/ retrieval purposes. The Blast occurred due to failures in maintenance, management, testing, and operation

Drill operates through a hole in the hull

Several wells drilled from one platform (rig)

Directional drilling is required to access several locations in the formation

Sonic equipment is used to determine drilling sites most likely to produce oil

Mobile Offshore Drilling Unit (MODU) used to dig a well

Guiding stands of drill pipe into fingers at top of derrick

Shifts (crews and operation)

Organisational structure

Hierarchical structure

Role responsibility

Crew assignments and allocations

Crew Members

Management

Regulator

Cooking and Cleaning Crew

Supervisors, Foreman, Leading Hands, Superintendents

Limited number of operational personnel per shift

Congested

Highly complex

Technological

Strictly operational

Small

Control Rooms

Small living/ resting quarters

Self-sufficient platform

Cost production

Mass production of oil per day (approx 100k+ barrels of oil

Comprises cranes for operational purposes (e.g. lift containers, pipelines etc.)

Staff handover/ transfer of information required by internal policy

Rig Design Rooms

Muster Station

Control Room

Kitchen

Laundry

Social/ Games

Helicopter Platform

Crane Area

Fire Room

Mandatory training

Training and qualifications required

Medical Staff

Engineers

Manual Laborours

Monitor viscosity and mud density while adding chemicals or oil-based fluids

Casing string were installed to drill well to a depth of 18k feet

Installation Manager

Monitor and ensure health/ well being of staff

Manage projects, tests, operations etc.

Safety performance, procedures, operations etc.

Rig

Drill Pipe Drill

Personnel

Organisational Factors (Management)

Equipment conditions

Critical decision making

BP site leaders decided to continue production after negative pressure test

Job Design

Designed to drill in water depths of up to 10k feet

Cement used as a barrier to seal the wellbore from the reservoir

  1. Wellhead seal assembly was installed and tested
  1. The first integrity test of the well (positive pressure test) was conducted by closing the blind shear rams and applying 2700 psi of pressure

Test confirmed integrity of blind shear rams, casing, seal assembly, and top wiper plugs

The shoe track which plays a key role in isolating hydrocarbons was NOT tested Shoe track

  1. Drill pipe was run to 8k feet in preparation for the second integrity test (negative pressure test)

Tests purpose was to place the well in a controlled under-balanced state to test all mechanical barriers

Test was conducting by displacing some mud in the well with a spacer, followed by seawater. After displacement the upper annular preventer was closed in attempt to bleed the system down to zero psi but fluid in the riser was leaking past the annular preventer

  1. Hydraulic closing pressure for annular preventer was increased to 1900 psi aimed to create a tighter seal against drill pipe

The riser was filled with up to 50 barrels of mud to replace the volume that had leaked past the annular

  1. The drill pipe valve was opened and the pressure reduced to zero, bleeding off 15-23 barrels of seawater
  1. Well site leader advised rig crew that negative test procedure needed to be conducted on the kill line to meet permeate requirements

Information Transfer

After second integrity test was conducted, site well leader informed rig crew that negative test procedure needed to be conducted on the kill line

Site well leader informed rig crew to conduct first integrity test

Drill pipe valve was closed and testing reconfigured for flow to be monitored on the kill line

Kill line valve was opened and seawater was bled off before it was closed again and then the drill pipe pressure gradually increased

  1. Seawater was pumped into the kill line to confirm it was full but the kill line was routed to the mini trip-tank and less than 1 barrel was bled from the kill line where the flow stopped

Drill pipe valve was to be closed, tested, and reconfigured for flow and monitored on the kill line

Kill line valve was opened then closed by rig crew and monitored for 30 minutes for flow but no flow showed

Signs of flow was monitored for 30mins but did not occur however the drill pipe pressure remained

Discussion around drill pipe pressure occurred and the source of the 1400 psi took place where it was explained as a phenomenon called the 'bladder effect;

No flow showed and test was deamed successful

Inadequate communication and understanding between rig manager and BP leader

Conversation between site well leader and rig crew regarding integrity testing was not communicated

As part of normal operations to temporarily abandon the well, the crew began to displace the remaining drilling fluid of seawater. The annular preventer was opened and the well returned to an overbalance position preventing further influx into the wellbore

Displacement continued as planned and the well went under-balanced resulting in pressure of the well dropping below the reservoir pressure

Well started to flow and crew emptied trip-tank which likely masked any flow indications on the flow meter

Failure

Constant pump rate pressure should have declined as the mud (heavier) was replaced with seawater (lighter). Instead pressure on drill pipe increased by 100 psi, indicating well problem

Sheen test on spacer is to check that no free fluid will be discharged to the sea. The pumps were shut down when the spacer reached the surface. A machine test was performed and the spacer was determined to be suitable for discharge.

The drill pipe pressure continued to increase by the minute

Fluid returned from the riser was routed to the overboard depth line

All mud pumps were shut down before an attempt was made to bleed the drill pipe

Rig crew discussed the differential pressure on the drill pipe

Mud shot up through the derrick and the diverter was closed so flow was diverted to the mud gas separator when the rig crew closed an annular preventor

First gas alarm sounded

Combustible gas cloud reached the aft starboard quadrant of main deck and entered air intakes for engine rooms. The main power generation engines went into over-speed, shutting off all electrical power and controls.

Two explosions ocurred

Rig crew attempt to shut in the well and disconnect the lower riser package from the BOP stack

Emergency disconnect sequence for the BOP was activated from the bridge. While lights changed on the control panel, no flow was observed on the flow meters

Emergency disconnect system did not function when activated and the lower marine riser package failed to unlatch from the BOP which did not seal the well

When disconnection from the well failed, order to abandon the rig was called

Riser

BOP BOP

Casing

Reservoir

Environment

Sea Floor

Wellbore

Sea Pressure

Hydrocarbons Hydro

Energy/ Force

Failure to recognise hydrocarbons entered well

Shoe track barriers did not isolate hydrocarbons

Hydrocarbons entered well undetected and well control was lost

Negative pressure test was accepted although the well integrity was not established

Influx and hydrocarbons were not recognised until they were in the riser

Influx was not apparent until hydrocarbons were in the riser

Well control response actions failed to regain control of the well

Decision to divert mud gas separator resulted in gas venting onto the rig

Fire and gas system did not prevent hydrocarbon ignition

Blowout Preventor emergency modes did not seal the well

Annular cement barrier did not isolate hydrocarbons

Centralizer

BP rely on service provider to determine an appropriate cement slurry for the well

BP responsible for assuring cement slurry providers work and accepting proposal

Halliburton (service provider) did not conduct comprehensive lab tests that could have identified problems with cement product

BP decided to use six centralisers and a long string production casing in the well which is consistent design to others. This decision increased likelihood of channeling above the main hydrocarbon zone

BP and Halliburton could have improved technical assurance, risk management, and change management could have altered decision making on outcome

Shoe track has two types of mechanical barriers:
1- Cement in shoe track
2- Double check valves in float collar

Hydrocarbons bypassed float collar check valves as they were damaged

Negative test was conducted to confirm the integrity of the annulus cement, shoe track, casing, and wellhead seal assembly

Increase in pressure on drill pipe should have lead to further inquiry by personnel regarding integrity of well rather than test result assumed to be attributed to a phenomenon known as the 'bladder effect'

Negative test was deamed a success by BP and transocean rig personnel

3 drill pipe pressure increases/ indicators were recorded with no well control actions taken

Well must be shut in upon influx and if necessary, hydrocarbons diverted safely away from the vessel. Response by rig crew was not 'typical' in accordance with training and awareness of control events

Diverter was closed and routed flow to mud gas separator

Annular preventer was activated which did not seal the well

In a well control event, the riser converter can be closed and the fluids directed

Gas dispersed rapidly across the rig

Gas entered engine room through air intakes

Engines went into over-speed, resulting in loss of power

Emergency systems failed to seal the well after initial explosion

Initial explosions and fire damaged the control cables (MUX Cables) and hydraulic lines which caused emergency disconnect system failing to activate the blind shear ram which was triggered by personnel on the bridge

Diverted to mud gas separator

Communication was lost and resulted in various decisions (including unauthorized or trained) to occur

AMF did not complete due to to MUX cable damage

Weaknesses and testing/ maintenance of BOP was evident

Well site leader was aware something was wrong and did not wish to proceed with normal operations, instead wanted to wait until more testing could verify mechanical accuracy.
BP responsible for encouraging operations to continue and disregard pressure increase on drill pipe

Audit findings relating to maintenance found that the sub-sea personnel recorded well control equipment maintenance manually on separate spreadsheets and in a daily logbook instead of in the Maintenance Management System

The lower, middle, and upper BOP ram bonnets had not been re-certified since 2000. The OEM recommended re-certification period is 5 years

Maintenance records did not substantiate that it was compliant with 5-year replacement policy for high-pressure holes/ equipment

Maintenance records were not accurately reported in maintenance management system

BOP complete record tracking of specific individual components was not achieved

19 known modifications to the BOP and its control system were identified

19 known modifications occurred which changed the functionality of the BOP, but likely did not contribute to accident

Hydraulic system leaks, solenoid valve coil faults etc. should have been detected by BOP diagnostic capability that was available to rig crew and sub-sea personnel through routine testing/ maintenance requirements

Continuous psi pressure rise through tests and operation

High pressure BSR function is one of six emergency methods that may have reduced/ prevented the accident. This is crew-initiated but was not achieved.

EDS function is crew initiated (rig personnel) from a control panel which was designed to mitigate the risk of losing containment but was not activated

AMF is designed to to mitigate risk caused by a catastrophic failure of the riser which had to be manually armed by rig personnel from BOP control panel but did not function

Rig crew attempted normal mode of BOP system operation using an annular preventer prior to accident

Control room operators

Sub-sea personnel

Control room management

Ground floor senior manager

Maintenance records were not accurately reported where conditions of critical components were not discovered until after the accident

Six leaks were identified in the hydraulic system

Whilst testing requirements were in accordance with policy/ industry standards, intervention systems tests were not conducted at the surface as required by company policy

Diagnostic practices did not recover all critical components of the control system and were not utilised effectively to detect control system defects

Recommendations

Procedures and Engineering Technical practices

Update and clarify current practices to ensure clear and comprehensive cementing guidelines are available and controlled

Clearly defined mandatory practices

Recommended practices and operational guidance

Definitions of critical cement jobs

Description of technical authority's (TA's) role

Establish minimum requirements for ram types, numbers, capability, emergency well control activation systems

Update relevant technical practices

Testing and Review

Review and understand the purpose of the tests

Define barriers to be tested

Identify and evaluate consequences of failure

Develop contingency plan of action in failure events/ likelihood

Develop detailed procedure that requires comprehension

Clearly define success and failure criteria for tests

Apply authorisation instructions if results are outside defined success criteria

Management

Review/ assess effectiveness of risk management and change management processes

Develop/ implement action plan to address areas of improvement

Define minimum standard of functional teams to deliver quality performance

Assess high-consequence drilling activities

Provide regular training to all staff on Incident and Emergency Response (IERP) procedures

Develop and conduct Crisis Management Procedure where Crisis Management Team (CMT) are allocated roles and understand responsibilities

Competency

Review all critical zones of isolation engineering plans and procedures

Implement assurance and technical services including quality/ comprehension to industry standards

Implement competency programs to deepen capabilities of personnel in operational and management/ lead positions

Review current personnel level of knowledge, proficiency and determine necessary training for professional development (PD)

Schedule and conduct high-level audits for safety, quality, and system/ operational compliance and verify/ correct audit findings

Establish leading and lagging indicators for well integrity/ operational performance including well control and safety critical equipment

Solenoid valves/ pods were modified and miswired

Miswiring caused battery to drain

2 x coils of electrical wire designed to work together to generate a magnetic field to operate the valve
1 x coil failed

Flow rate